Results of dielectric measurements on K-11 switchgear bushings on E.M.L. system (TM-ETR-74)

Last updated on 31 March 2014 3:04
Following the explosion at Wolverton feeder station on 6 Mar 76 due to a bushing failure in the K-11 switchgear, dielectric measurements have been carried out on bushings in a number of other switching stations which are known from previous work to contain suspect bushings, For the past three years,...
Author(s): Bradwell A;Bates GA;Billinge RH
Organisation(s): British Rail Research ;
1976
United Kingdom
Log in or register to continue
Register for free individual access
  • Unlock research, articles and more
  • Get updates on RSSB’s activities